
And since, due to the narrow confines of the motor mount and the tight fit of the hole that I already enlarged to fit the bigger manifold some months back, I was unable to fit the filter directly to the carb inlet, so I used a couple inches of the rubber tube from the original air intake. It looked like this:

Replacing the curved tube, and readjusting the air mixture got me right back to where I had been in the first place. And I tried adjusting the mixture 3 different times with test jaunts up my block, all unsuccessfully.
I'm stumped. I can not believe that bit of curved hose makes so much difference in the performance but I can't figure out which way to go with the carb and its jets and adjustments to get it running right. The hard part of course is that you can't get the poor performance when its sitting on the centerstand, the engine must be under load.
Maybe it needs a different sized pilot jet. I suppose bigger would be the way to go but that is just a guess. Any suggestions?
BTW, I did bypass the fuel shutoff with a new length of hose after replacing my curved inlet pipe and made one run up the hill successfully without the engine cutting out. I think that verifies that the valve is bad. I'll be awaiting the new one in the mail shortly. Thanks Alan!
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